Colin's Radio Control

Very small version of Dragonfly with 3D printed parts and Illuminati 32 flight controller.


Type Tricopter Home made
Receiver OrangeRX R720x V2 7 channel
 Ch1 Roll  
 Ch 2 Pitch  
 Ch 3 Lift  
 Ch 4 Yaw  
 Ch 5 Mode Acro / Auto-Level / Heading Hold / Head-free / Altitude Hold
 Ch 6 Barometer   
Ch 7    
Flight Controller Quanum Illuminati 32  
Battery 3S LiPo  
ESCs Turnigy MultiStar 20A BLHeli-S
Motors  FC 2812 1534 kv  
Circumdiameter 70 cm  


Takeoff Weight 1085g Including 2200mAh 3S LiPo


Some flights on 11th August 2020

I built this tricopter last year. The first few flights were a complete disaster!

The tricopter was virtually uncontrollable and took a lot of fighting with the sticks to get it in the air at all. No amount of PID tuning helped at all.

At first I thought that I had damaged the flight controller as I had had a lot of problems flashing the firmware on the Illuminati 32s. I decided to leave this one and use it for parts in a future project. 

During the current coronavirus lockdown I thought I would have one last look before dismantling it. It was only then that I noticed that one of the spars was slightly warped and the port motor was not level.

A couple of washers under the motor mount soon had the motor level.

I reset the PIDs to default, checked all the Cleanflight settings, recalibrated the accelerometer and tried another test flight. Hey! It flew great. After a bit of PID tuning it is now one of my most stable copters.

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